![]() |
To day I send 2 hours on the dyno to test 2 mods that I did in 2011. Normaly I always do a dyno session after any power mod but
|
|||||||
|
|
LinkBack | Thread Tools | Display Modes |
|
|
#7 (permalink) |
|
A True Z Fanatic
Join Date: Oct 2009
Location: Canada
Posts: 1,156
Drives: 370z
Rep Power: 25 ![]() ![]() ![]() ![]() ![]() ![]() ![]() ![]() ![]() ![]() ![]() |
To day I send 2 hours on the dyno to test 2 mods that I did in 2011.
Normaly I always do a dyno session after any power mod but since last year I was plaged with the ECU pulling timing and not knowing it untill I blew the tranny on the drag strip. The flywheel was badly cracked, which we think it was affecting the knock sensor to not be happy thus pulling timing ! It was difficult to have much of any consistense pull after pull but since the flywheel got replaced, I do not have any problem with that ! Soo today was to confirm 2 mods. 1= HR vs VHR intake manifold (you can see my picture when I did the conversion) ![]() - 2= Throttle Body OEM stock @ 60mm VS bored at 62.5mm The AFR were ajusted before the recording pull.
|
|
|
| Bookmarks |
|
|
Similar Threads
|
||||
| Thread | Thread Starter | Forum | Replies | Last Post |
| MEGAN RACING: SS Downpipes! | G&M Performance | Drivetrain/Engine | 8 | 07-25-2011 12:50 PM |
| Megan Drift CBE - my 2 cents | Vince's Red-Z | Intake/Exhaust | 14 | 02-26-2011 07:51 PM |
| Megan Racing Exhaust | tyler20c | Intake/Exhaust | 3 | 01-07-2011 12:59 PM |