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Originally Posted by DrBacon Really hard to tell with it still on the car but it appears to be the same size as the one on the supercharger, definitely larger

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Old 10-08-2019, 10:54 PM   #1 (permalink)
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Originally Posted by DrBacon View Post
Really hard to tell with it still on the car but it appears to be the same size as the one on the supercharger, definitely larger than 3". I really doubt there's a restriction in my exhaust, but who knows anymore. If I'm making almost 13psi at 7,100 rpm before it starts to fall off (because of either boost leak or belt slip, or both...) I can't even imagine what it would be trying to do if it hit redline at 7,700rpm. What the hell lmao
If your using the Art pipes paired with the E370 (but there are two versions of it, not sure which one your running with but I guess it is the one they designed for forced induction according to your description to the pipe diameters), I don't think there isn't enough free flowing. I'm also running Art pipes but using a true-dual 3" catback exhaust. What's your average exhaust gas temperature under WOT?
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Old 10-08-2019, 11:16 PM   #2 (permalink)
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If your using the Art pipes paired with the E370 (but there are two versions of it, not sure which one your running with but I guess it is the one they designed for forced induction according to your description to the pipe diameters), I don't think there isn't enough free flowing. I'm also running Art pipes but using a true-dual 3" catback exhaust. What's your average exhaust gas temperature under WOT?
I don't have an EGT probe, so I don't know. I have a very hard time believing this could be exhaust flow related, as I'm sure there's others with more restrictive exhausts that don't have similar problems. At worst case scenario if I can't figure this out, I'll just unbolt the damn thing and do a pull and see what happens.

Here's a picture of the pulley setup:
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Old 10-08-2019, 11:47 PM   #3 (permalink)
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Originally Posted by DrBacon View Post
I don't have an EGT probe, so I don't know. I have a very hard time believing this could be exhaust flow related, as I'm sure there's others with more restrictive exhausts that don't have similar problems. At worst case scenario if I can't figure this out, I'll just unbolt the damn thing and do a pull and see what happens.

Here's a picture of the pulley setup:
Looks like the stock 3.2 jackshaft sc pulley. Is that the brass shipping plug on the right side of the sc? It doesn't look like the 3/16" allen head dipstick cap.
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Old 10-08-2019, 11:49 PM   #4 (permalink)
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Looks like the stock 3.2 jackshaft sc pulley. Is that the brass shipping plug on the right side of the sc? It doesn't look like the 3/16" allen head dipstick cap.
The one on the right is the dipstick, the one on the left is the vent plug.
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Old 10-08-2019, 11:58 PM   #5 (permalink)
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The one on the right is the dipstick, the one on the left is the vent plug.
Good, just wanted to make sure.
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Old 10-09-2019, 01:15 AM   #6 (permalink)
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Originally Posted by DrBacon View Post
I don't have an EGT probe, so I don't know. I have a very hard time believing this could be exhaust flow related, as I'm sure there's others with more restrictive exhausts that don't have similar problems. At worst case scenario if I can't figure this out, I'll just unbolt the damn thing and do a pull and see what happens.

Here's a picture of the pulley setup:
Looking good. There seems to be no belt dust. Check if there is leak from the intake pipes, silicone hoses, gaskets, and/or valve. I'm always interested in the design and actual performance of the E370, especially its 2-1 Y section where there seems to be only one single 3-3.25" pipe as the merge collector. I think it does help advance the scavenging effect but dunno if this will cause back pressure to hinder CFM of big power. From their web info, it seems the exhaust is capable of supporting 700-hp output. Let us know the dyno results and type of fuel you use when you have them (if possible). Guess this is the only way to justify the hypothesis of the restriction (whether it does flow freely or not).
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Last edited by "Z"en; 10-09-2019 at 07:53 AM.
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Old 10-09-2019, 08:05 PM   #7 (permalink)
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Looking good. There seems to be no belt dust. Check if there is leak from the intake pipes, silicone hoses, gaskets, and/or valve. I'm always interested in the design and actual performance of the E370, especially its 2-1 Y section where there seems to be only one single 3-3.25" pipe as the merge collector. I think it does help advance the scavenging effect but dunno if this will cause back pressure to hinder CFM of big power. From their web info, it seems the exhaust is capable of supporting 700-hp output. Let us know the dyno results and type of fuel you use when you have them (if possible). Guess this is the only way to justify the hypothesis of the restriction (whether it does flow freely or not).
I was planning on doing the dyno next week, the local shop has an opening, however I did a small 4th gear pull and it feels like my poor stock clutch is already trying to slip. I need to take care of that first unfortunately, it would just be a waste of money if it slips while on the dyno. I did around 4 data logged full throttle pulls today, and checked around the belts and there is zero rubber/belt dust anywhere that I could see. The boost pressure is seemingly inconsistent, I really don't trust this MAP sensor so I'm ordering a boost gauge now. According to the MAP sensor I hit 0.80 bar (11.6psi) at anywhere from 6,300 to 6,600 rpm. The last pull I did peaked at 0.90 bar (13psi) at 6,800 before again, falling off to around 0.80 bar by redline.
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Old 10-09-2019, 08:23 PM   #8 (permalink)
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Alright guys, car just had everything installed, NO TUNE has been uploaded yet.
MAFS and throttle bodies are connected correctly. My Tech found similar issues here online and thought a proper tune being uploaded or a recalibration of throttle bodies will correct, but tuner says it won’t. You guys have any ideas?

Thanks!
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Old 10-09-2019, 11:33 PM   #9 (permalink)
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Originally Posted by Senna-F1 View Post
Alright guys, car just had everything installed, NO TUNE has been uploaded yet.
MAFS and throttle bodies are connected correctly. My Tech found similar issues here online and thought a proper tune being uploaded or a recalibration of throttle bodies will correct, but tuner says it won’t. You guys have any ideas?

Thanks!
Are these OEM MAFs, TBs, wires, cables, and connectors? Had they cleaned before install and startup? Which extension cables are you using? I'd ask my mechanic to check these first, followed by checking the TPS. Make sure your using the OEM wires, connectors, and the Stillen Gen2 extension cables. As long as they are fully functional, I see no reason the TBs can't be calibrated through the learning process.
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Old 10-10-2019, 11:00 PM   #10 (permalink)
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Originally Posted by Senna-F1 View Post
Alright guys, car just had everything installed, NO TUNE has been uploaded yet.
MAFS and throttle bodies are connected correctly. My Tech found similar issues here online and thought a proper tune being uploaded or a recalibration of throttle bodies will correct, but tuner says it won’t. You guys have any ideas?

Thanks!
So we decided to upload tune anyway to see if it would get rid of these codes, and it did. Just FYI for future searches.
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Old 10-09-2019, 11:53 PM   #11 (permalink)
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Originally Posted by DrBacon View Post
I was planning on doing the dyno next week, the local shop has an opening, however I did a small 4th gear pull and it feels like my poor stock clutch is already trying to slip. I need to take care of that first unfortunately, it would just be a waste of money if it slips while on the dyno. I did around 4 data logged full throttle pulls today, and checked around the belts and there is zero rubber/belt dust anywhere that I could see. The boost pressure is seemingly inconsistent, I really don't trust this MAP sensor so I'm ordering a boost gauge now. According to the MAP sensor I hit 0.80 bar (11.6psi) at anywhere from 6,300 to 6,600 rpm. The last pull I did peaked at 0.90 bar (13psi) at 6,800 before again, falling off to around 0.80 bar by redline.
Sounds like a plan. Keep us posted if possible. I'd still suggest you have an EGT gauge and sensor installed. Will help you keep your engine and exhaust in check under WOT.
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Old 10-11-2019, 05:16 PM   #12 (permalink)
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Sounds like a plan. Keep us posted if possible. I'd still suggest you have an EGT gauge and sensor installed. Will help you keep your engine and exhaust in check under WOT.
I think the drop in boost at high rpms is from the supercharger side belt slipping. I ran my hand under under the belts and on serpentine side it's clean, but once I touch that supercharger side belt my hand is covered in black dust which I assume isn't normal and due to it slipping. I can tighten that tensioner, which looks like a real pain in the *** to get to while still in the car, however if it's already making 13psi with belt slip I really don't want to know what it will do once it's tightened. Boost gauge arrives next week and I should be able to verify with that the MAP sensor readings just to make sure. Also new clutch is going in next week as well
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Old 10-11-2019, 05:35 PM   #13 (permalink)
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I think the drop in boost at high rpms is from the supercharger side belt slipping. I ran my hand under under the belts and on serpentine side it's clean, but once I touch that supercharger side belt my hand is covered in black dust which I assume isn't normal and due to it slipping. I can tighten that tensioner, which looks like a real pain in the *** to get to while still in the car, however if it's already making 13psi with belt slip I really don't want to know what it will do once it's tightened. Boost gauge arrives next week and I should be able to verify with that the MAP sensor readings just to make sure. Also new clutch is going in next week as well
Chances are it isn't going to make any more boost, it'll just make 13 psi all the way to redline. Keep an eye on the supercharger side and see if you start to get dust build up around the pulleys and bracket.
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