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This is the latest Dyno I took to verify my butt Dyno... I knew something was off. The squealing sound, I don't know yet, it could be the washers I
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#18 (permalink) |
Premium Member
![]() Join Date: Oct 2011
Location: Tampa
Posts: 4,142
Drives: 13' Magma Red Nismo
Rep Power: 7335 ![]() ![]() ![]() ![]() ![]() ![]() ![]() ![]() ![]() ![]() ![]() |
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This is the latest Dyno I took to verify my butt Dyno... I knew something was off.
The squealing sound, I don't know yet, it could be the washers I had in my front crash bar to add clearance. I'll see if it disappeared. ![]() This was the last tune in May... It looks a bit rough compared to my previous tune. It's definitely not nearly as smooth and down 10lbft of TQ. ![]() Car is at the shop. First pull was 315. They took the bumper off and it was at 320. He didn't give me the tq number. He took the log data and sent it to my tuner. They're saying the VVEL is acting up with the tune after 5600rpm. I guess there is an ecutek setting to fix that. I'm still waiting to get the car back. Btw, here's a pic of the new stuff I decided to order an F.I. crash bar hoping it would give at least the same clearance as a modified crash bar as well as giving me some breathing room with the oil cooler. ![]()
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Old Car:GTM TSC'd 550whp / 410lbft tq @ 11.88PSI
New Car: Under Construction ![]() Last edited by SS_Firehawk; 08-20-2017 at 08:44 AM. |
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