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Old 05-12-2011, 11:35 PM   #226 (permalink)
98intrigue
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Quote:
Originally Posted by Red__Zed View Post
You figure the TB issue is related to using different intake tract lengths?
That is the culprit to the MAF maxing out, but we are not sure why it threw a code for a bad throttle body. It would make sense that since the driver's side MAF was getting about 20% more air than the passenger side MAF, maybe the driver's side throttle body was trying to compensate and open more than then it through a code and went into limp mode? But then why after hooking it all back together about 2 hours later, it ran fine...even after probably 5 dyno pulls?
Quote:
Originally Posted by Ryan@prosportGauges View Post
im still wondering why not mount the MAF's before the Split to each TB!
Because then Shawn would have to modify both intake piping and relocate the BOV... if the upgraded MAFs don't work out, your idea will be the next step.
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