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I will have this complete Modshack cooler setup for sale, with the newly custom made hoses real soon, as I am getting the new Stillen one for their front bumper if anyone is interested. I'm thinking 300 shipped. The new hoses were 110 by themselves.
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It worked great here all of last late summer and fall at some hot track days. |
Is it possible that the hoses while filled with oil got so heavy that after many miles of up-and-down movement, they separated? I am asking as in looking at the pics, they run horizontal but there is no mention of any bracing/brackets to hold the weight?
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Hose Blow-off analysis
What we know: 1) Both Socketless and Braided hoses have separated in 3 reported instances. Not sure if Travis's was hose related, so that could be 4 2) Neither of those hose types and attachment styles have regularly reported failure rates. 3) Both hose/end styles are rated well above the expected temps and pressures What we don't know: 1) install specifics/variables. One of the comments from the Jack above stuck in my mind: The hose needs significant slack.. Both Cab and Mike report they had slack in their installs. I have no reason to doubt that. One thing not taken into consideration is the Torquing of the motor on it's mounts. Under acceleration and compression braking, the motor could be moving around the axis of the mounts by as much as an inch. Certainly in Mike's case, under track conditions, this could be even more. As the motor rocks on it's mounts, alternate stretch and compression forces are applied to the fitting. I suspect enough of these cycles, with a tad too little slack, and the barbs wore through the inner hose liner. At that point the structural integrity of the hose was gone and it blew off. But I had enough slack you say...Alternate theory #2: The hose, as laid out, passes under the sway bar. Lottsa clearance when up on a lift, not so much when on the ground. Compound that with a lowered car (CAB, not sure of your suspension) and you may have the sway bar working and flexing on the hose close to the fitting. This may potentially cause a similar failure by compromising the inner liner. Be sure the hoses are routed to cross under the swaybar close to the pivot point to minimize this. I'll put some cautions up on page one. I'd also recommend, on new builds, extending the hose lengths by 1" as Mike did after his incident. (My dimensions quoted BTW are cut end to cut end and DO NOT include the fitting.). It is always best to actually make up the hose lengths by fitting to the particular install before final socketless (or other) end assembly. A little too short and you run the risk of hose failure because of the above. |
Modshack,
Excellent summary. I agree with you, engine torquing under track day or extreme driving events could be as much as 4-5 inches. Couple this with hose contraction of up to 10% reinforces how critical the routing and length of a plumbing be calculated. Jack RPW |
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Steve |
Oil cooler installs
I think we are getting a little crazy on the oil cooler hose bit. As I said in a previous post I spent 23 years in Jet Enginge Test Research and Development. We used aeroquip hoses that were CRIPMED as we had our own shop with the tools to do so. We made sure that hoses were not too long and or too short. We used high temp anti chaffing clamps to route the hoses. Any where that we thought chaffing was a possibliity we added that protection.
My position on this is do right the first time, don't try to reengineer a simple process. You can order the stainless steel crimped hoses with the cooler or have hoses made at say, Napa or at any hydraulic shop that makes hoses in your area to the proper length. The torqueing of the engine and its result on the hoses to me is a mute point if they are clamped and routed properly. Spend a couple of more bucks and time and you will not have to worry if you are going to dump your oil or not. The pilot of a Jet fighter dose not have time to worry about things like that. Yes the jet engine does at times have premature failures and their RPMS are 50-60K not 8K. |
modshack, good analysis, as always... +rep
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I've got a question for you experienced modders out there. How much should I torque down the AN fittings for those lines that are supplied from the GTM kit? I am currently getting a little seepage from the edge of where the fittings meet the steel braided line. Is this something to be concerned about? When I get her back up on stands, I will take some pics and post (though that probably will not happen until at the earliest the evening of Tuesday - 9 March).
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I think I went about a 1/2 turn after snug or something. Don't remember exactly... Don't have any seepage though lol.
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We are only working with a low presure system. The leaking or weeping at the hose and braid says to me that the hose is not properly installed on the fitting (cut straight) piece of braid has overlapped the hose end or has a bend to close to the fitting that it has distorted the shape of the hose on the fitting and for me I think that that the latter is the main problem with hoses popping off. Aluminum fittings can be over torqued and strip the threads unlike stainless. Snug up the fitting and take 1/4 final turn. On pipe threads always use teflon tape. Start 1/16-1/8" back from end start to wrap counter clockwise and only take 2 wraps, don't over do it. Becarefull that no tape over laps the end of the fitting as this will get cut off and get into the system. If you remove a pipe fitting with teflon tape on it use a soft wire brush (tape will become clear after use and you may not notice it )to remove excess teflon tape, do not just tape over the fitting. Inspect the other fitting end for left over teflon and remove any that has been left behind if not this stuff will make its way into the system when you reinstall the fittings. Check your routing and clamping make sure that the bends are not severe. |
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